The International Space Station 2B Photovoltaic Thermal Control System (PVTCS) Leak: An Operational History
[摘要] As early as 2004, the Photovoltaic Thermal Control System (PVTCS) for the International Space Station's 2B electrical power channel began slowly leaking ammonia overboard. Initially, the operations strategy was "feed the leak," a strategy successfully put into action via Extra Vehicular Activity (EVA) during the STS-134 Space Shuttle mission. This recharge was to have allowed for continued power channel operation into 2014 or 2015, at which point another EVA would have been required. In mid-2012, the leak rate increased from 1.5lbm/year to approximately 5lbm/year. As a result, an EVA was planned and executed within a 5 week timeframe to drastically alter the architecture of the PVTCS via connection to an adjacent dormant thermal control system. This EVA, US EVA 20, was successfully executed on November 1, 2012 and left the 2B PVTCS in a configuration where the system was now being adequately cooled via a different radiator than what the system was designed to utilize. Data monitoring over the next several months showed that the isolated radiator had not been leaking, and the system itself continued to leak steadily until May 9th, 2013. It was on this day that the ISS crew noticed the visible presence of ammonia crystals escaping from the 2B channel's truss segment, signifying a rapid acceleration of the leak from 5lbm/year to 5lbm/day. Within 48 hours of the crew noticing the leak, US EVA 21 was in progress to replace the coolant pump - the only remaining replaceable leak source. This was successful, and telemetry monitoring has shown that indeed the coolant pump was the leak source and was thus isolated from the running 2B PVTCS. This paper will explore the management of the 2B PVTCS leak from the operations perspective.
[发布日期] 2014-05-05 [发布机构]
[效力级别] [学科分类] 航空航天科学
[关键词] [时效性]